As promised here's a update of where we're at on this project.
Once we had all of the shmoo cleaned off of the chassis I had Larry polish the tunnel. Here he's just getting started wet sanding the second side of the tunnel. In the end I don't think it turned out too bad.
IMAG0597 by
nick 80lf, on Flickr
IMAG0596 by
nick 80lf, on Flickr
Once he had the tunnel shined up we moved to the track. If you'll remember this track had a broken cleat and 2 bent cleats. We were able to straighten the 2 bent cleats and replaced the one broken cleat. Here Larry is giving the track half of the patented Brock Weber treatment (we didn't remove all the cleats though).
2015-11-22_07-09-01 by
nick 80lf, on Flickr
The first part to go back on the chassis was the steering bracket. We intended to work on the sled during the Thanksgiving holiday with the main task being to have a rolling chassis. As luck would have it we made an attempt to install the drive shaft the Tuesday before Thanksgiving. Of course, we discovered Mrs Claus messed up last Christmas and one of the drive shaft bearings was incorrect. Normally I only use SKF bearings for drive shafts but I made an exception and stopped at the Deere dealer the day before Thanksgiving and picked up the correct one (with 30 minutes to spare before they closed). Once this was behind us we dropped the skid in. Well.......it was more like wrestle the skid in. It wasn't until we had all of the bolts started that I was able to snap a photo of Larry tightening the skid bolts with the cordless impact.
2015-11-27_03-58-40 by
nick 80lf, on Flickr
Then we assembled both skis and installed them on the chassis. Which was where we left off after the Thanksgiving holiday.
2015-11-27_03-59-05 by
nick 80lf, on Flickr
The next few weeks were pretty much wasted do to my stupidity. I found a really cheap source for stamped tie rod ends. Turns out many go cart suppliers carry these and they are about 75% cheaper than the power sport suppliers. Well you can also buy an entire tie rod kit. I thought sure why not........turns out these were back ordered (even though the place I ordered them from claimed they had them in stock) after about 4 weeks they showed up and........both ends of the tie rod were right hand thread........dohhhhhh. So we scrapped that idea and cleaned up the originals.
This is where we started at the beginning of the Christmas holiday. We did manage to install the carbide rods, snow flap, handle bars (with poly handwarmers) and fuel pump, while the stupidity of the tie rod saga was unfolding.
2015-12-24_08-20-09 by
nick 80lf, on Flickr
After we had the tie rods sort of in we dropped the motor into place and then encountered everyone's worst nightmare.......the dreaded Kawasaki recoil. Up till this point I've been fortunate and never had one of these apart. Honestly I'd heard the stories of others and thought to myself "it's just a recoil....it can't be that bad". This recoil was in perfect working order the only thing was the cord was a little short and greasy. So I thought....we'll just pull the cord out all the way, I'll hold the pulley in place and he can replace the old cord with new.......wrong. We quickly learned we had to take the pawls out to get the old rope out. I'd love to meet the genius that said "hey let's put five springs under this little plate and laugh as they try to put it all back together". Eventually we got it but not without scuffing the paint job on the recoil so we had a little touch up to do.
2015-12-24_08-19-31 by
nick 80lf, on Flickr
The following day we made a run to the hardware store to pick up new bolts for the outer tie rods so here's Larry tackling that project.
2015-12-26_02-07-47 by
nick 80lf, on Flickr
Once that was complete the brake disk and caliper went on next.
2015-12-26_10-10-44 by
nick 80lf, on Flickr
The tank and air box are just sitting on the sled in this photo so we could get an idea of the fuel line routing. Cleaning the fuel tank has been quite the project. In the past I've gotten away with rinsing them out with some type of water based de-greaser. The varnish on the upper part of this tank had dried out and become very hard. We eventually put a few gallons of kerosene in the tank with a bottle of Seafoam and a few handfuls of BB's and have been shaking it for the last few weeks. I think it's just about to the point where it could be rinsed out.
Hopefully we'll get the opportunity to work on this a little more on new years day.