Kohler engine.
stock Walbro carb.
high speed needle was set at 3/4 turns out (as per the owner's manual).
low speed needle was turned out an additional 1/4 turn to eliminate low-end "bogging" (worked nicely then).
Gas is 91 octane @ 44:1 with Honda HP2 synthetic (sticker on tank says "John Deere oil @ 50:1....").
Motor is tight; not whipped out.
Worried it may be a bit lean, so I opened up the high speed another 1/4 turn, and will take the sled out tomorrow and check the plugs again. There is not a single speck of black or shiny aluminum (the dreaded "melting piston") on either plug. I know how to do a "plug check", so the motor was not allowed to idle before I hit the kill button.
Opinions?
![Image](http://i54.photobucket.com/albums/g92/kari_D/DSC01066.jpg)